CN106701115A - Coke ovenlow pressure ammonia valve changing method for preventing gas discharging - Google Patents

Coke ovenlow pressure ammonia valve changing method for preventing gas discharging Download PDF

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Publication number
CN106701115A
CN106701115A CN201510786795.8A CN201510786795A CN106701115A CN 106701115 A CN106701115 A CN 106701115A CN 201510786795 A CN201510786795 A CN 201510786795A CN 106701115 A CN106701115 A CN 106701115A
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CN
China
Prior art keywords
pressure
temperature
high pressure
ammonia
pressure ammonia
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Pending
Application number
CN201510786795.8A
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Chinese (zh)
Inventor
彭磊
贾磊
程志海
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Angang Steel Co Ltd
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Angang Steel Co Ltd
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Publication date
Application filed by Angang Steel Co Ltd filed Critical Angang Steel Co Ltd
Priority to CN201510786795.8A priority Critical patent/CN106701115A/en
Publication of CN106701115A publication Critical patent/CN106701115A/en
Pending legal-status Critical Current

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Abstract

The inventionprovides a coke ovenlow pressure ammonia valve changing method for preventing gas discharging. Before changing, the pressure of a gas collecting tube is set to a lower limit of 95-105 Pa; when the temperature of the gas collecting tube is too high so that the pressure surge greatly exceeds an upper limit, a manual operation is performed at the scene; a high pressure ammonia valve with a corresponding oven number is opened with a small open degree of 1/5-1/4, and high pressure ammonia is temporarily used to replace the low pressure ammonia to cool raw coke oven gas; during the changing process, the opening degree of the high pressure ammonia valve is less than 1/4, to ensure the pressure in a coking chamber is higher than the pressure of a combustion system at the same level; after the change is completed, the high pressure ammonia valve is closed in time to prevent the temperature of the gas collecting tube from continuously increasing. The invention can greatly shorten the valve change time, and reduce the raising of the temperature of the gas collecting tube and pressure surge, thereby effectively avoiding environmental pollution caused by coke oven discharging, preventing the pipe fitting of the gas collecting tube from being damaged, and reducing costs for replacement parts.

Description

A kind of coke oven low-pressure ammonia penstock replacing options for preventing coal gas diffusion
Technical field
The invention belongs to coking field, more particularly to a kind of coke oven low-pressure ammonia penstock for preventing coal gas diffusion is more Change method.
Background technology
Raw gas temperature is changing low pressure ammoniacal liquor generally 80~100 DEG C after ammoniacal liquor sprinkling cooling in discharge Can only a certain section of discharge be carried out stopping ammoniacal liquor operation during valve, because the activity duration is long, Header temperature 400 DEG C or so can be increased to, from equation of gas state PV/T=K (K is constant), work as gas temperature When T changes, the volume of gas starts free wxpansion, and discharge is a rigid confined space, gas collection body Product V immobilizes, then the rising of raw gas temperature T, directly results in collecting main pressure P risings, makes this The pressure of section raw coke oven gas locally increases, and causes the pressure distribution inside whole discharge uneven.Automatic regulating machine In regulation, gas collection overpressure amplitude of variation is larger, and regulation caused collection not in time easily occurs in discharge Tracheae is diffused, substantial amounts of raw coke oven gas effusion, causes serious environmental pollution.In addition, discharge and accessory May cause pipe fitting drawing crack because temperature is raised.
The content of the invention
The present invention is intended to provide one kind can shorten the replacing valve time, Header temperature and pressure oscillation are reduced, Avoid the occurrence of the coke oven online replacing options of low-pressure ammonia penstock that coke oven emission and discharge pipe fitting are damaged.
The present invention prevents the specific method that the coke oven low-pressure ammonia penstock of coal gas diffusion is changed from being:
(1) the low-pressure ammonia penstock for damaging is changed when selection stops production, it is to avoid coke pushing coalings operation to more Change the influence of operation;
(2) before low-pressure ammonia penstock is changed, collecting main pressure is set in 95~105Pa of lower limit, works as gas collection Pipe temperature is too high when causing pressure oscillation to exceed the upper limit greatly, and scene beats manually operated, it is to avoid automatically adjust too late The coal gas diffusion and Ignition Phenomena of Shi Zaocheng;
(3) the high pressure aqua ammonia valve of correspondence heat (batch) number is opened using 1/5~1/4 small guide vane, high pressure is used temporarily Ammoniacal liquor substitutes low pressure ammoniacal liquor and raw coke oven gas is lowered the temperature;
(4) during replacement operation, high pressure aqua ammonia valve opening is no more than 1/4, it is ensured that charing chamber pressure is high In same absolute altitude combustion system pressure, and without negative pressure appearance;
(5) high pressure aqua ammonia valve is closed after replacement operation is finished in time, prevents Header temperature from continuing to raise.
Beneficial effects of the present invention are:
The measure such as lower the temperature is carried out to raw coke oven gas due to substituting low pressure ammoniacal liquor using high pressure aqua ammonia, can greatly shorten valve Door replacing construction, reduces Header temperature and raises and pressure oscillation, coke oven emission occurs and makes so as to be prevented effectively from Into environmental pollution, it is therefore prevented that the damage of discharge pipe fitting, reduce spare part expense.
Specific embodiment
The specific method that coke oven low-pressure ammonia penstock of the present invention is changed is:
1st, the low-pressure ammonia penstock for damaging is changed when selection stops production, it is to avoid coke pushing coalings operation to changing The influence of operation.
2nd, before low-pressure ammonia penstock is changed, collecting main pressure is set in 95~105Pa of lower limit, works as discharge Temperature is too high when causing pressure oscillation to exceed the upper limit greatly, and scene beats manually operated, it is to avoid automatically adjust not in time The coal gas diffusion and Ignition Phenomena for causing.
3rd, the high pressure aqua ammonia valve of correspondence heat (batch) number is opened using 1/5~1/4 small guide vane, high pressure ammonia is used temporarily Water substitutes low pressure ammoniacal liquor and raw coke oven gas is lowered the temperature.
4th, during replacement operation, high pressure aqua ammonia valve opening is no more than 1/4, it is ensured that carbonizing chamber pressure is higher than With absolute altitude combustion system pressure, and without negative pressure appearance.
5th, high pressure aqua ammonia valve is closed after replacement operation is finished in time, prevents Header temperature from continuing to raise.
Meanwhile, preliminary preparation should be carried out before replacing, the activity duration is shortened as far as possible, to prevent discharge The too high pipeline drawing crack phenomenon for causing of temperature.

Claims (1)

1. a kind of coke oven low-pressure ammonia penstock replacing options for preventing coal gas diffusion, it is characterised in that specific side Method is:
(1) the low-pressure ammonia penstock for damaging is changed when selection stops production, it is to avoid coke pushing coalings operation to more Change the influence of operation;
(2) before low-pressure ammonia penstock is changed, collecting main pressure is set in 95~105Pa of lower limit, works as gas collection Pipe temperature is too high when causing pressure oscillation to exceed the upper limit greatly, and scene beats manually operated, it is to avoid automatically adjust too late The coal gas diffusion and Ignition Phenomena of Shi Zaocheng;
(3) the high pressure aqua ammonia valve of correspondence heat (batch) number is opened using 1/5~1/4 small guide vane, high pressure is used temporarily Ammoniacal liquor substitutes low pressure ammoniacal liquor and raw coke oven gas is lowered the temperature;
(4) during replacement operation, high pressure aqua ammonia valve opening is no more than 1/4, it is ensured that charing chamber pressure is high In same absolute altitude combustion system pressure, and without negative pressure appearance;
(5) high pressure aqua ammonia valve is closed after replacement operation is finished in time, prevents Header temperature from continuing to raise.
CN201510786795.8A 2015-11-17 2015-11-17 Coke ovenlow pressure ammonia valve changing method for preventing gas discharging Pending CN106701115A (en)

Priority Applications (1)

Application Number Priority Date Filing Date Title
CN201510786795.8A CN106701115A (en) 2015-11-17 2015-11-17 Coke ovenlow pressure ammonia valve changing method for preventing gas discharging

Applications Claiming Priority (1)

Application Number Priority Date Filing Date Title
CN201510786795.8A CN106701115A (en) 2015-11-17 2015-11-17 Coke ovenlow pressure ammonia valve changing method for preventing gas discharging

Publications (1)

Publication Number Publication Date
CN106701115A true CN106701115A (en) 2017-05-24

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CN (1) CN106701115A (en)

Cited By (3)

* Cited by examiner, † Cited by third party
Publication number Priority date Publication date Assignee Title
CN106701110A (en) * 2015-11-17 2017-05-24 鞍钢股份有限公司 Method for stabilizing pressure of gas collection pipe of coke oven
CN107671790A (en) * 2017-09-30 2018-02-09 中国二十冶集团有限公司 A kind of online replacing options of coke oven valve body
CN107723011A (en) * 2017-11-13 2018-02-23 鞍钢股份有限公司 A kind of method that online Water Cutting of negative pressure coal gas system pulls hole

Citations (3)

* Cited by examiner, † Cited by third party
Publication number Priority date Publication date Assignee Title
JPH06322371A (en) * 1993-05-11 1994-11-22 Nippon Kasei Chem Co Ltd Apparatus for automatically changing over valve in smokeless charging apparatus of raw material coal in coke oven
CN101066518A (en) * 2007-06-08 2007-11-07 神华乌海煤焦化有限责任公司 Coke oven coal loading dedust system
CN104449777A (en) * 2013-09-24 2015-03-25 上海梅山钢铁股份有限公司 Operating method with zero emission of coke-oven gas for newly-built coke oven of coke oven system in service

Patent Citations (3)

* Cited by examiner, † Cited by third party
Publication number Priority date Publication date Assignee Title
JPH06322371A (en) * 1993-05-11 1994-11-22 Nippon Kasei Chem Co Ltd Apparatus for automatically changing over valve in smokeless charging apparatus of raw material coal in coke oven
CN101066518A (en) * 2007-06-08 2007-11-07 神华乌海煤焦化有限责任公司 Coke oven coal loading dedust system
CN104449777A (en) * 2013-09-24 2015-03-25 上海梅山钢铁股份有限公司 Operating method with zero emission of coke-oven gas for newly-built coke oven of coke oven system in service

Non-Patent Citations (1)

* Cited by examiner, † Cited by third party
Title
董传舰等: "《3#4#焦炉循环氨水管道的不停产切换》", 《苏、鲁、皖、赣、冀五省金属学会第十五届焦化学术年会论文集(上册)》 *

Cited By (6)

* Cited by examiner, † Cited by third party
Publication number Priority date Publication date Assignee Title
CN106701110A (en) * 2015-11-17 2017-05-24 鞍钢股份有限公司 Method for stabilizing pressure of gas collection pipe of coke oven
CN106701110B (en) * 2015-11-17 2019-05-31 鞍钢股份有限公司 A kind of method of stable coke oven collecting main pressure
CN107671790A (en) * 2017-09-30 2018-02-09 中国二十冶集团有限公司 A kind of online replacing options of coke oven valve body
CN107671790B (en) * 2017-09-30 2019-06-21 中国二十冶集团有限公司 A kind of online replacing options of coke oven valve body
CN107723011A (en) * 2017-11-13 2018-02-23 鞍钢股份有限公司 A kind of method that online Water Cutting of negative pressure coal gas system pulls hole
CN107723011B (en) * 2017-11-13 2020-09-01 鞍钢股份有限公司 Method for online water cutting of hole-pulling of negative pressure gas system

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